Wednesday, August 23, 2023
If you can't be behind the windshield, the next best place to be is volunteering!
Monday, July 31, 2023
LuckyDog @ Brainerd International Raceway
1st in class, 3rd overall. We ran a clean race, and everything ran like clock work. I went out first, had a great start, and put distance on many competitors. I went into fuel conservation mode for much of the race; shifting at 6500rpms, and short shifted into 4th gear between turn 6 and 7 and kept it there all the way until turn 12. This allowed my stint to get us to the two hour mark, which put on the 3 pit stop strategy. I had a great battle w/ Craig Silver from Silver Martini, in their NB Miata, which should have more power. I lead him for dozen laps, he eventually got past me, and I chased him hard for another 10 laps, then got around him eventually, and we both ended up going in for fuel. We did have the rare occurrence where the entire race was red-flagged due to lightning in the area. We finished 1st in class and14 seconds away from 2nd overall. The 2nd place car with five minutes left on the clock broke, during that fine minutes we closed the gap and finished on the same lap. During the nightly mechanic checkup we found out we had a broken lug stud! A rear wheel bearing started giving signs it was time to go. We also burnt through an entire set of front Hawk "Endurance" brake pads! :O
Day two we were not so lucky. We knew no matter what we would not be able to make the 3 pit stop strategy, so we figured might as well run harder and faster, knowing we would be doing 1 hour 30 to 1 hour 40 minute pits. I started again, and had a relatively uneventful hour forty five in the car, ran pretty consistent 1.51 and 1.52 lap times. One driver went out and start saying the brakes and handeling where very weired. Turns out that same rear wheel bearing we swapped out the night before, that axle busted right at point of the axle nut! We swapped the axle and got the car back out in 30 minutes. Another driver said the windshield was getting hard to see out of, which turned out happened to be because the car ejected the oil fill cap!!! Even with those two unfortunate visits into the pit we finished 4th place in class, 7th over all.
$2,500 was raised for Brainerd's local Sharing Bread Soup Kitchen.
Official results can be found: here.
Tuesday, May 30, 2023
Mechanical Drama....partial race report from SCCA Harvey West Regional race 05/27
My rebuilt motor arrived from X-Factor as part of a group buy. I decided it would be a good idea to run a Mazda Motorsports baffle. It is a steel sheet that sits in the bottom of the oil pan to help oil stay down at the oil pick up. It doesn't add any power, it simply helps prevent oil starvation. Seems like decent insurance to me. I ordered one from Mazda, except it never showed up. Turns out the person taking the order messed up the credit card order and never bothered to communicate that. Well by the time I figured this out, I couldn't wait any longer. I remembered having something in my original motor, and thought fine, I will pull it from the non-leaking motor and transplant it. So the refurbished motor had the oil pan pulled off. The old motor had its oil pan pulled off, then only to find out this was all for not, as it did not have the baffle! Ugg…clean, re-RTV, new gasket, and re-assemble, kick myself for burning up an entire Saturday afternoon.
The motor gets installed, and the very first time it gets fired up and sounded HORRIBLE! So much so, for a few seconds I thought it might be a rod knock. I have dealt with a number of cars over the years that have had bad lifters, I’ve installed fresh lifters before. I have heard lifter tick many times, and usually it goes away in short order. Not this time. I had two friends come by and give it a listen and confirm that after a 2nd heat cycle that it didn’t sound good. Oil pressure using 5w-30 with a water temp of 180 degrees was about 13psi (oil pressure gauge goes from “0” to a halfway mark, then 25psi so, not the most accurate.
We pulled the entire subframe to get the oil pan off. FYI with a Miata to get at the oil pan one has to pretty much remove the motor from the car, or remove the oil pan to get the oil pan off. Everything looked fine; the pickup tube was clear, the pick-up tube gasket was indeed there. Ugg…clean, re-RTV, new gasket, and re-assemble. Pulled off the valve cover, check that all of the hydraulic lifters seemed fine and had good spring tension. No issues found, add assembly lube to all the cam lobes, fill with 10w-30. Let it run for a bit, the noise is better, but not great. The following day, it sounded perfect! I have never owned a Miata that was quiet and smooth.
Come back the following weekend to find a puddle of oil on the floor. <sigh> Pull the transmission out, replace the rear main seal and the rear “half-moon” oil pan gasket. Reassemble, let the RTV cure for six hours, let it do a heat cycle, a short test drive, and all seems well!
The following week load it up on the trailer, and let it idle, and notice oil drops on the trailer. <sigh> Get to HiTech in Elk River for dyno tuning. Their tailpipe sniffer wide band oxygen sensor was being all sorts of wacky, and my AEM wideband was also doing its own thing. So I have invalid air/fuel numbers to go by. The dyno operation was either having a bad day, is generally just cranky, or hates Miatas? I got four runs, and settled on 14ish degrees of timing and 40lbs of fuel pressure. Resulting in 122whp and 119tq, which is 8 more HP than the previous motor, which doesn’t sound like a lot, but percentage wise is a decent chunk.
Friday was a test day at Brainerd International Raceway. I ran the first session, short shifting at 6500 rpms. Came in and checked the car over to find the bottom of the car covered in oil. <sigh> The transmission was pulled again! A fellow Miata racer pointed out that sometimes there can be a ridge on the crankshaft where the main seal rides from wear. The proposed solution was to install the main seal 1/16 of an inch proud (or sticking out) vs. having it flush. Thus the seal will ride on a part of the crank that is not worn down.
The next morning we finished the reassembly, ran the practice session. Everything seemed fine. Changed out the oil used for “break-in” for a mix of Schaeffer's 10w30 & 20w50 Series 9000 racing oil. My qualifying session was cut short as on the 4th lap the exhaust separated where the down pipe meets the exhaust. I used up my last spare gasket, and borrowed one from Jenkins Racing. FYI the 1.6l and 1.8l gasket are not the same, but I made it work anyways.
Twice I had the igniter wire fall off of the starter. I can tell you getting all buckled in to the car, all the accessories hooked up, then the calls to grid come over the PA, then the car doesn't start; it doesn't do any good for ones mental state!
The first race I had a phenomenal start and finished okay. Oil pressure at wide open even towards the end of the race was always around 30psi. However when back in the pit, the motor had a horrible lifter tick even after letting the it idle for a few minutes with the radiator fan running and the water temp sitting at 180 degrees.
Sunday, practice, qualifying, and the race went okay. The best lap time I could do was a 1 minute 50, which is good for me, but still a second off of my best lap time. The wind was quite strong all weekend, but I still would have expected to best previous lap times with the extra power.
I struggled with putting the power down coming out of turn 13. I still chronically over break for turns 3 and 7. Turn 12 still continues to be a pucker factor for me. After each session I would wipe off a couple of drops of oil from the bell housing of the transmission. So I am unclear if that is residual from the previous leakage, despite cleaning it pretty good or if it is still leaking.
HUGE thankyous to Geoff, George, Jenkins Racing for helping and not letting me throw the towel in (SEVERAL TIMES!). Also to my wife and Andy Nash.
More photos and videos to come...